After several days playing with the PID settings on the KK2 board, I finally got a good day to maiden the PVC V-Tail. It started off really nice, even the yaw turn looked good. After I let it fly up high and tried to bring it back towards me, all went to hell. Motor #3 broke its zip-ties and I was able to fix that really easily. However, motor #4 started acting up and then it stopped altogether. I think that the motor was sporadic and may have caused the crash. Not sure :-(
Well, I don't have another DT750 motor so i decided to pull off all the electronics and use them for a new DIY multirotor project I am working oin. Video on that coming soon!!
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